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Failure Analysis of the Guyed-V Tower Link Plate Deformation of a 500 kV Transmission Line
- Source :
- E3S Web of Conferences, Vol 252, p 02029 (2021)
- Publication Year :
- 2021
- Publisher :
- EDP Sciences, 2021.
-
Abstract
- Component analysis, mechanical property test, field survey and finite element mechanical calculation were used to analyse and evaluate the deformation failure of the Guyed-V Tower link plate of a 500 kV transmission line. The results show that the main cause of the failure is the relaxation of the guy after right front guy or wire is subjected to a large impact towards the large side. The weak design of the link plate structure and the misfitting of angle steel are the indirect causes of the failure. The construction angle of anchor cable is larger than the design value, and the tension of anchor cable is low, which has a certain impact.
- Subjects :
- Environmental sciences
GE1-350
Subjects
Details
- Language :
- English, French
- ISSN :
- 22671242
- Volume :
- 252
- Database :
- Directory of Open Access Journals
- Journal :
- E3S Web of Conferences
- Publication Type :
- Academic Journal
- Accession number :
- edsdoj.78620f7afa4420bd9e66a3595e96b5
- Document Type :
- article
- Full Text :
- https://doi.org/10.1051/e3sconf/202125202029