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Failure Analysis of the Guyed-V Tower Link Plate Deformation of a 500 kV Transmission Line

Authors :
Liu Weike
Cao Xianhui
Hu Yujing
Li Dong
Xie Yi
Source :
E3S Web of Conferences, Vol 252, p 02029 (2021)
Publication Year :
2021
Publisher :
EDP Sciences, 2021.

Abstract

Component analysis, mechanical property test, field survey and finite element mechanical calculation were used to analyse and evaluate the deformation failure of the Guyed-V Tower link plate of a 500 kV transmission line. The results show that the main cause of the failure is the relaxation of the guy after right front guy or wire is subjected to a large impact towards the large side. The weak design of the link plate structure and the misfitting of angle steel are the indirect causes of the failure. The construction angle of anchor cable is larger than the design value, and the tension of anchor cable is low, which has a certain impact.

Subjects

Subjects :
Environmental sciences
GE1-350

Details

Language :
English, French
ISSN :
22671242
Volume :
252
Database :
Directory of Open Access Journals
Journal :
E3S Web of Conferences
Publication Type :
Academic Journal
Accession number :
edsdoj.78620f7afa4420bd9e66a3595e96b5
Document Type :
article
Full Text :
https://doi.org/10.1051/e3sconf/202125202029