1. Investigation of the effectiveness of velocity string to improve gas well productivity.
- Author
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Zhai, Zhongbo, Qi, Shiwei, Kartoatmodjo, Gayatri, Wang, Taiji, Wang, Junfeng, and Bo, Jiangwei
- Subjects
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GAS wells , *STEADY-state flow , *MULTIPHASE flow , *VELOCITY , *LIQUEFIED gases , *SENSITIVITY analysis - Abstract
Velocity string (VS) is one of the most common methods to unload water in gas-producing field. In order to understand the behavior affecting production rate, we obtained several parameters including well completion, gas well production data, gas liquid ratio (GLR) and pressure data at tubing and casing head pressure, flowing bottom hole pressure. We then explore the relationship between these parameters against reservoir pressure and perform sensitivity analysis using multiphase steady-state flow simulator to analyze the parameters are the most sensitive to gas production rate. The results show that: (1) at larger inner diameter of the VS, there is a certain increase trend of gas production of gas wells. However, the production rate does not show a linear increase relationship with the larger internal diameter. It will reach certain inflection point before it decreases; (2) the gas production of the VS well is mainly driven by the reservoir pressure, the higher the reservoir pressure, the greater the gas production; (3) the root cause of relatively low initial production rate after small inner diameter coiled tubing VS installation is categorized as an abnormal well startup. This study provides theoretical support for selecting the optimum size and depth of VS to maintain well productivity. [ABSTRACT FROM AUTHOR]
- Published
- 2024
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